G
gyd23
Guest
My name is Gydeon, i am an F-15 Crew Chief in the USAF, and on March 12, 2011 I bought my first DSM - A 1997 Mitsubishi Eclipse GSX
:thumb:
now there was only 3 issues with the body of the car when i bought it
1. the driver side side marker was gone, "magically" fell out.
2. the clearcoat is fading on top, and some slight dings/chips here and there on the car.
3. this fairly big ding on the fender:
so the very first thing and pretty much only thing i did so far was pick up some smoke side markers for it..
So after i bought this car with a fresh engine in it (around 20 miles on it just from putting a temporary pre-lim tune on it) and having it un-tuned I planned to baby it untill i hit at least 500 miles and got a good tune done on it. (yes i know 500 miles isn't sufficient enough for a break in but this engine was only taken apart for the rods & crank to be replaced so it was all already broken in other than those.) and right about the 250 mile mark on about the 3rd day I noticed the timing belt doing this:
I don't know if you all can tell but it started walking itself towards the outside of the cam gears.. oh so very slightly, since i haven't been around 4 cyl more specifically this engine long enough to know if that was ok or not and briefly looking over the timing system that i could see, like the tensioner, making sure its all aligned and seeing nothing abnormal i drove on.
At almost the 400 mile mark i was almost home from working with my recruiter and i started hearing a slapping noise under the hood and immediately after a loud BANG (like a balloon popping) OMG
hdamn:
Turns out i threw the timing belt, while partially shredding it, and i knew for sure judging by the timing ^^.. that i threw valves, and was just hoping that my pistons were OK. So i took everything apart, i found out what was wrong, and also what went wrong.
Yes i know that post isn't supposed to come out of the Motor Mount bracket. So i consulted the guy i bought the car from and unfortunately he didn't know of this, because frankly he didn't have the car long enough to notice this fault. But someone before him had purposely pressed this pin out, why i don't know but they did and it eventually walked itself back out. He told me to go find a bracket somewhere and that any 1G bracket will work, turns out a 1G bracket won't work due to the motor mount bolt holes, so i took my bracket that had broke up to a small engine repair shop that i am familiar with and had him pull the post out about 1/16 and put a nice weld bead on the back of it and smooth it out, and i got a 1/16 thick washer to put around the post and under the normal washer to compensate for the gap the arm would make. Worked out perfect.
I then bought new valves, got new ones put in etc. and threw it back together. Something i didn't know about at the time was that the CAS controls ignin timing and i just kind of bolted it back on where it looked like it was before. (not so good of an idea.) but i started her up and she ran just like before. Still wouldn't idle due to being un-tuned and not having an IAC. but all was good, so i drove it around for a couple more days babying it untill i got it tuned. Then, got it tuned at Pure Tuning in Toledo, OH. off the bat it was doing pretty good minus the fact he couldn't get it to idle right. it was very temperamental and would idle good for a couple mins then want to die or randomly want to idle at 2,000 RPM.
after the 19psi successful tune and unsuccessful 24psi tune when the car started missfiring, we trouble shooted for a little bit: replaced coil pack, wires, and plugs.. then gave up with the thought it was miss firing due to either: ignition control module, CAS, or possibly because theres a bad wire to the water temp sensor which supposedly help controls ignition timing.
and even till now in mid April still don't know what is wrong. more trouble shooting and fixing i will do soon. :applause:
:thumb:


now there was only 3 issues with the body of the car when i bought it
1. the driver side side marker was gone, "magically" fell out.
2. the clearcoat is fading on top, and some slight dings/chips here and there on the car.
3. this fairly big ding on the fender:

so the very first thing and pretty much only thing i did so far was pick up some smoke side markers for it..


So after i bought this car with a fresh engine in it (around 20 miles on it just from putting a temporary pre-lim tune on it) and having it un-tuned I planned to baby it untill i hit at least 500 miles and got a good tune done on it. (yes i know 500 miles isn't sufficient enough for a break in but this engine was only taken apart for the rods & crank to be replaced so it was all already broken in other than those.) and right about the 250 mile mark on about the 3rd day I noticed the timing belt doing this:


I don't know if you all can tell but it started walking itself towards the outside of the cam gears.. oh so very slightly, since i haven't been around 4 cyl more specifically this engine long enough to know if that was ok or not and briefly looking over the timing system that i could see, like the tensioner, making sure its all aligned and seeing nothing abnormal i drove on.
At almost the 400 mile mark i was almost home from working with my recruiter and i started hearing a slapping noise under the hood and immediately after a loud BANG (like a balloon popping) OMG


Turns out i threw the timing belt, while partially shredding it, and i knew for sure judging by the timing ^^.. that i threw valves, and was just hoping that my pistons were OK. So i took everything apart, i found out what was wrong, and also what went wrong.





Yes i know that post isn't supposed to come out of the Motor Mount bracket. So i consulted the guy i bought the car from and unfortunately he didn't know of this, because frankly he didn't have the car long enough to notice this fault. But someone before him had purposely pressed this pin out, why i don't know but they did and it eventually walked itself back out. He told me to go find a bracket somewhere and that any 1G bracket will work, turns out a 1G bracket won't work due to the motor mount bolt holes, so i took my bracket that had broke up to a small engine repair shop that i am familiar with and had him pull the post out about 1/16 and put a nice weld bead on the back of it and smooth it out, and i got a 1/16 thick washer to put around the post and under the normal washer to compensate for the gap the arm would make. Worked out perfect.
I then bought new valves, got new ones put in etc. and threw it back together. Something i didn't know about at the time was that the CAS controls ignin timing and i just kind of bolted it back on where it looked like it was before. (not so good of an idea.) but i started her up and she ran just like before. Still wouldn't idle due to being un-tuned and not having an IAC. but all was good, so i drove it around for a couple more days babying it untill i got it tuned. Then, got it tuned at Pure Tuning in Toledo, OH. off the bat it was doing pretty good minus the fact he couldn't get it to idle right. it was very temperamental and would idle good for a couple mins then want to die or randomly want to idle at 2,000 RPM.
after the 19psi successful tune and unsuccessful 24psi tune when the car started missfiring, we trouble shooted for a little bit: replaced coil pack, wires, and plugs.. then gave up with the thought it was miss firing due to either: ignition control module, CAS, or possibly because theres a bad wire to the water temp sensor which supposedly help controls ignition timing.
and even till now in mid April still don't know what is wrong. more trouble shooting and fixing i will do soon. :applause: